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cleat

Got another one. A 416 this time.

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cleat

Hydraulic hose grommet ready to be installed.

1105763221_Hydraulichosegrommetreadytobeinstalled.JPG.4567936fc87bfc44a698ee145c851f98.JPG

 

Hydraulic hose grommet installed.

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Hydraulic supply line temporary plug removed, ready for valve installation.

2135254718_Hydraulicsupplylinereadyforvalveinstallation.JPG.3a578f78b90841e10b7b8fc0a2c5444f.JPG

 

Hydraulic valve assembly ready to be installed.

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Hydraulic valve assembly installed.

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Hydraulic hoses ready to connect to cylinder.

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Hydraulic hoses connected to cylinder.

1947348625_Hydraulichosesconnectedtocylinder.JPG.0f597fa3424fef02cf69c9720e8a2614.JPG

 

Hydraulic return line ready to be installed.

1119397571_Hydraulicreturnlinereadytoinstall1.JPG.741eb7178d019e8f0e6fb8b3e0c5a8d2.JPG

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Hydraulic return line installed.

454807726_Hydraulicreturnlineinstalled.JPG.193ab721aa7265f8439a34e1668ea3a2.JPG

 

Hydraulic lines and fittings tightened at valve.

477383647_Hydrauliclinesandfittingstightenedatvalve.JPG.7b9e65f399477536f16ee7c73ebdef7e.JPG

 

Hydraulic lines and fittings tightened at filter adapter.

1173411955_Hydrauliclinesandfittingstightenedatfilteradaptor.JPG.df050f99f8ae5c72fb04008b65221b4d.JPG

 

Hydraulic supply line tightened at pump.

1352817483_Hydraulicsupplylinefittingtightenedatpump.JPG.f7b2e72d7ad81b6cfeba9b398c84c91a.JPG

 

Overview as of today.

2029429533_OverviewasofDec102025.JPG.a4f023e1c874834aeba84134d18e8b7c.JPG

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cleat

Hydro belt tension pivot rod assembly ready to be installed.

1837083044_Hydrobelttensionpivotrodassembly.JPG.96b2e35fe38a7d39f15b9524c8bec1b3.JPG

 

Hydro belt tension pivot rod bushing installed.

120497315_Hydrobelttensionpivotrodbushinginstalled.JPG.ac4fa48ccc92fbd2fa6b5f0f156c3d51.JPG

 

Hydro belt tension pivot rod wave and flat washers installed.

1143635239_Hydrobelttensionpivotrodwaveandflatwashersinstalled.JPG.0fe1817939a335a4fcc532f2728a481f.JPG

 

Hydro belt tension pivot rod greased at pivot points.

1309541094_Hydrobelttensionpivotrodgreased.JPG.66b8cea6080fa19bcc972d264bb140ec.JPG

 

Hydro belt tension pivot rod spring installed.

1583868962_Hydrobelttensionpivotrodspringinstalled.JPG.1110eee3ecfa7ecf740194cef7f116fa.JPG

 

Hydro belt tension pivot rod slid into bushing and hoodstand.

Spring slid onto anchor bolt and nut spun on finger tight.

429130599_Hydrobelttensionpivotrodandspringinstalled.JPG.12c2fd63494852b092f077442db1e825.JPG

 

Hydro belt tension pivot rod washer and E clip installed.

190251112_HydrobelttensionpivotrodEclipinstalled.JPG.dbbcfcae5914fffb1401fe306f39f096.JPG

 

Hydro belt tension spring nyloc nut turned in until excess play is removed but spring is not clamped tight.

1336966340_Springnylocinstalled.JPG.c36d867059a74c0e24c9383a02daf5c2.JPG

 

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cleat

Snow storm from last Wednesday knocked out our internet and that was still out this morning when the power went out.

Power came back on after 4 hours. Luckily it was only -9 out so the house only cooled down to 15 degrees C.

When the power came back on the satellite dish also had melted off so I now have power and internet.

My post yesterday was through my phone that works so long as I am standing just outside the shop.

 

 

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cleat

Parking brake lever assembly ready to install.

I am installing an early style as I do with all of my builds as I don't like the later style with the plastic knob on the left side.

266075114_Parkingbrakeleverassemblyreadytoinstall.JPG.6ee39aa735db0a60dddaa72ade2a5f45.JPG

 

Parking brake bolt, washers, and spacer installed.

Never seize on the SS bolt.

2106908740_Parkingbrakeboltwashersandspacerinstalled.JPG.8e74e7dadb2f9f53453d57044a3f2939.JPG

 

Parking brake lever assembly installed and nut torqued to 30 ft/lb.

491794515_Parkingbrakeleverassemblyinstalled.JPG.9e75220247a1fbeaa22342dbfaba61df.JPG

 

Parking brake lever spring installed.

1589578249_Parkingbrakeleverspringinstalled.JPG.e8a731bb4d2fecc287e263825226da92.JPG

 

Shift cover plate sat in place to verify parking brake lever location.

I cut out the slot for the parking brake earlier this past summer.

1853257228_Shiftcoverplatesatinplacetoverifyparkingbrakeleverlocation.JPG.f4dfad637a27eb6d418b4bb5c4261486.JPG

 

Adjusted brake spring according to manual.

717892619_Brakeadjustment.JPG.252fa0758f2c318f64c0b92a34ddc05b.JPG

 

Edited by cleat
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cleat

Front fender bracket ready to install.

Note the large washers that will hopefully prevent the Hoodstand from cracking again.

1411802094_Frontfenderbracketreadytoinstall1.JPG.9a3e000a784ea29204b6c48aff053056.JPG

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Front fender bracket bolted into place just loose enough that it will move around.

2082087984_Frontfenderbracketinstalledandboltstorquedto204in-lb.JPG.0670e91b81efb12f2b54998b92c1a632.JPG

 

Fender sat on to verify bracket placement.

Turns out front fender bracket needs to be moved forward as far as possible for the holes to all line up.

1795753236_Fendersatontoverifyholeslineup.JPG.b94fb213081fb4d633cbaf3e6eefed51.JPG

 

I then removed the fender and checked to be sure the front fender bracket is square by measuring to the hoodstand as shown.

Both sides were 7-7/8" so good there.

1040200137_Frontfenderbracketmeasuringtoverifyitissquare1.JPG.23059ec009c31d862714e39b40cfc2db.JPG

1851125305_Frontfenderbracketmeasuringtoverifyitissquare2.JPG.bad54cb4639917d76e28e5f94e818651.JPG

 

I then measured side to side from hoodstand to outer edge of front fender bracket.

Just over 2-3/4" both sides.

701656874_Frontfenderbracketmeasuringtoverifyitiscentered.JPG.eabe6f96f16d15d4a2dc77ae437c660f.JPG

 

Front fender bracket bolts torqued to 204 in/lb.

Shown here are the large washers installed.

They are different only because that is all I had on hand.

1103234709_Frontfenderbracketinstalledshowingwashersandnylocnut1.JPG.ed1629bb4c7db316c6fb73dc941dc58f.JPG

383441370_Frontfenderbracketinstalledshowingwashersandnylocnut2.JPG.d388953445546b630a54c79086a8540e.JPG

 

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ebinmaine

Precision 

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Handy Don
10 minutes ago, cleat said:

 

image.png.03c9119aad6de137271df80e2eaa44fb.png

This close tolerance would bug me until I’d emoved and shortened the bolt. :confusion-shrug:

And I am not nearly as meticulous as you are!

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cleat
38 minutes ago, Handy Don said:

image.png.03c9119aad6de137271df80e2eaa44fb.png

This close tolerance would bug me until I’d emoved and shortened the bolt. :confusion-shrug:

And I am not nearly as meticulous as you are!

 

Sorry, the camera angle made it look close.

I can actually fit a finger between the bolt and the hydraulic line.

DSCN9726.JPG.6030d84706504666146878fec2d3d251.JPG

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cleat

As recommended by Handy Don, I replaced the 5/16 x 1" bolt with a 5/16 x 3/4" bolt.

It protrudes through the nyloc by a full thread so it is good to go.

DSCN9727.JPG.1185d1822f113643f0f42bea0982157f.JPG

DSCN9728.JPG.3dc7726c9a676b4c4e65e046a417f13b.JPG

 

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Handy Don
43 minutes ago, cleat said:

As recommended by Handy Don, I replaced the 5/16 x 1" bolt with a 5/16 x 3/4" bolt.

It protrudes through the nyloc by a full thread so it is good to go.

And you “just happened” to have that shorter bolt on hand. I’m still in awe of your work! ;)

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cleat
1 hour ago, Handy Don said:

And you “just happened” to have that shorter bolt on hand. I’m still in awe of your work! ;)

 

One of the advantages of working at a large company (DuPont) and having my site shut down after cutting the maintenance department down to just me as the sole millwright is I got to take home truckloads of hardware.

This is a bit of it.

DSCN9729.JPG.7a206a236289b31fc361a3ff704dc93e.JPG

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DSCN9735.JPG.c4324f1b8cf9705ab20e304e21ee20bd.JPG

 

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lynnmor

I worked for Dupont for 11 years, then they sold off the electronics division.  Some made off with a considerable amount of stuff as they were floundering, I got very little.  Anyway, leaving that zoo and operating my own tool & die shop was the best move for me.

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cleat
14 minutes ago, lynnmor said:

I worked for Dupont for 11 years, then they sold off the electronics division.  Some made off with a considerable amount of stuff as they were floundering, I got very little.  Anyway, leaving that zoo and operating my own tool & die shop was the best move for me.

I worked for DuPont for 30 years. Started off making freon R12 then the plant got re-tooled to make Suva 123 after R12 was banned. I was in the end the only mechanic left servicing the entire plant.

 

Made lots of overtime but the 80 hour work weeks were hard. When they had to stop making Suva, the new replacement refrigerant plants were built in China I assume to get around environmental laws.

 

I am retired now and it is the best job ever.

 

 

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Handy Don

It is interesting what companies decide to “discard."

In the 80’s. my manager decided to upgrade to a newer model of Apple Laserwriter after buying one for $000’s only 18 months earlier (she had a budget surplus she wanted to spend). I tried to shop the “retired” unit around to other departments but no one wanted it (most of the company was using Windows). She got an approved “discarded asset” form from her manager and instructed me to deal with it. I drove in the next day and after carefully putting it on the loading dock and taking a picture (35mm film in those days), I picked it up and put it in my car. It served us at home for at least five or six years. Similar story for several cases of letter and legal copy paper deemed “unusable” by the tech support team after a couple of jams in the copier. Our family didn’t buy paper for printing for over 25 years after that. 

 

1 minute ago, cleat said:

I am retired now and it is the best job ever.

I call it the penultimate promotion. Glad you are enjoying it! :)

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cleat

PTO safety switch ready to bolt to bracket.

I had to re-use the old 4-40 nyloc nuts because I had no new ones.

2058158759_PTOsafetyswitchreadytobolttobracket.JPG.e67e400a69501381e383ef3128db0f29.JPG

 

PTO safety switch bolted to bracket.

972706748_PTOsafetyswitchboltedtobracket1.JPG.c2fbb94010975f79672b383d001686f5.JPG

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PTO safety switch assembly ready to be installed.

73427896_PTOsafetyswitchassemblyreadytobeinstalled.JPG.3d991f48e9ae42c6734b6e65595ae39d.JPG

 

PTO safety switch assembly installed.

Bolt tightened but not torqued.

976253578_PTOsafetyswitchassemblyinstalled2.JPG.1e98924a9874cec1f709346112c65c14.JPG

239790212_PTOsafetyswitchassemblyinstalled3.JPG.37f47af3b193ef63ee31c036202b8006.JPG

 

 

 

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cleat

Lift bar and chain ready to assemble.

Manual calls for a 5/16" bolt but lift arm is already drilled to accept a 3/8" bolt.

I just had to tap a taper punch into chain where bolt passes through to open it up slightly to fit the 3/8" bolt.

This will give a much more solid connection between bar and chain.

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Lift bar and chain assembled.

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Lift bar assembly ready to be installed.

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Lift bar greased at pivot points then bushing slid on.

1513072454_Liftbargreasedatpivotpoints.JPG.cddc1352ecf9e0e9bd39578e59c2b39c.JPG

 

Lift bar installed by first inserting left side of bar (with the bushing) into hole in left side of frame then aligning right side of bar with hole in right side of frame.

Push bar to the right as far as possible then while holding bar in this position, slide the bushing into the frame on the left side until it is filly seated.

596495406_Liftbarinstalledintoframeonrightside.JPG.e270ac63d6191aef478f61f51da31dd5.JPG

96178251_Liftbarinstalledandbushingslidintoplace.JPG.b19b3d3af4a0e7ff78c1177385c108b4.JPG

1792339122_Liftbarandbushinginstalled.JPG.9c494d0ce6cda24efafed3d7848d5553.JPG

 

Install the E clip to hold everything in position.

646969787_LiftbarEclipinstalled.JPG.96fe6af4abba61ca2a24e99dbcf7d298.JPG

 

Lift bar is now installed.

906821372_Liftbarinstalled.JPG.aea4529cc2d7d74c8e4808acef8d8816.JPG

 

Lift chain installed into bellcrank then washer and nyloc nut installed.

Nut screwed on a couple of turns but it's final adjustment is done after a deck is installed.

983908680_Liftchaininstalledintobellcrank.JPG.93c248828634834dcba630f32e6abab1.JPG

 

Lift bar washer and clip installed.

1426084319_Liftbarclipandwasherinstalled.JPG.8e5440cab253f4c00b465e29557e1f14.JPG

 

 

Edited by cleat
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Bill D
1 hour ago, cleat said:

PTO safety switch ready to bolt to bracket.

I had to re-use the old 4-40 nyloc nuts because I had no new ones.

2058158759_PTOsafetyswitchreadytobolttobracket.JPG.e67e400a69501381e383ef3128db0f29.JPG

 

PTO safety switch bolted to bracket.

972706748_PTOsafetyswitchboltedtobracket1.JPG.c2fbb94010975f79672b383d001686f5.JPG

1167731402_PTOsafetyswitchboltedtobracket2.JPG.70960c095d10bb05354ad33d240e8cca.JPG

1721321446_PTOsafetyswitchboltedtobracket3.JPG.049bc08b2ebc28792baffb7702c271a9.JPG

 

PTO safety switch assembly ready to be installed.

73427896_PTOsafetyswitchassemblyreadytobeinstalled.JPG.3d991f48e9ae42c6734b6e65595ae39d.JPG

 

PTO safety switch assembly installed.

Bolt tightened but not torqued.

976253578_PTOsafetyswitchassemblyinstalled2.JPG.1e98924a9874cec1f709346112c65c14.JPG

239790212_PTOsafetyswitchassemblyinstalled3.JPG.37f47af3b193ef63ee31c036202b8006.JPG

 

 

 

Shouldn't there be two switches?  One for the starter circuit and one for ignition?

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cleat
56 minutes ago, Bill D said:

Shouldn't there be two switches?  One for the starter circuit and one for ignition?

 

There were two originally as per this wiring diagram.

416 wire harness.pdf

 

However, I have simplified the wire harness and have eliminated the seat switch (that also tied into the second PTO switch) and also the neutral switch because the foot control auto returns to neutral.

This is how it is to be wired now.

416 wire harness modified.pdf

 

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cleat

Upper steering shaft ready for pre-install.

I will slide on an O ring to prevent washers and bushing from sliding down too far on initial setup.

707457446_Uppersteeringshaftreadyforpre-install.JPG.2b753d1eb88c753b2c1d1b7e0348934b.JPG

 

Upper steering shaft shim washers ready to be slid on.

1486017632_Uppersteeringshaftshimwashers.JPG.378f82ea1830752ad03fbdd032612923.JPG

 

Upper steering shaft O ring, shim washers, and bushing slid on.

1160736437_UppersteeringshaftOringshimwashersandbushingslidon.JPG.ed47930a542ba0b3b9b2846a50eb471f.JPG

 

Upper steering shaft installed into steering support block.

988745597_Uppersteeringshaftinstalledintosteeringsupportblock1.JPG.a148fcfec619caa23198bd3a43a11e8e.JPG

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Console ready to be installed.

1164174510_Consolereadytobeinstalled1.JPG.181074d07db748230283cdb48ab586cb.JPG

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Console temporarily installed.

1320300245_Consoletemporarilyinstalled.JPG.587a6f57f0bfd2b8a2afa061da43018a.JPG

 

Cotter pin just slid into hole with just enough shim washers to take up any free play.

1173539002_Cotterpininstalledwithjustenoughshimwasherstotakeupanyfreeplay.JPG.62e0363181b060ec669a44f0ae75840f.JPG

 

Console removed and stackup of shim washers above cotter cotter pin thickness measured to find a proper thickness washer.

1719409373_Shimwasherstackmeasuredtofindwasherthicknessrequired.JPG.361a6fae76a49ddc079e9109e9ec780a.JPG

 

Upper steering shaft greased on all contact areas.

706827428_Uppersteeringshaftgreasedforfinalassembly1.JPG.ce2a3e6c5fb14af4765347bc43085fcd.JPG

2118343485_Uppersteeringshaftgreasedforfinalassembly2.JPG.f5f6852b328953b7977de03e2c2ff30b.JPG

 

Lower steering shaft fan gear greased.

927562337_Lowersteeringshaftfangeargreased.JPG.a54f4d2dbc9188423d2510bd5fab7d3a.JPG

 

Lower steering shaft set perfectly level.

977026794_Lowersteeringshaftsetlevel1.JPG.ebcef86450461061372352ca77b9eb9f.JPG

559003184_Lowersteeringshaftsetlevel2.JPG.6db4fb6fedc7735a47e48d914f0ddddd.JPG

 

Upper steering shaft installed with a 1/4" pin punch in steering wheel wheel roll pin hole and aligned so punch sits level while ensuring lower steering shaft stays level.

This ensures proper gear mesh so steering wheel will be straight.

1976538295_Uppersteeringshaftinstalledandrollpinholealignedtobelevelusingapinpunch.JPG.8b99376f49d1faaa437e4129db4b71c5.JPG

 

Upper steering shaft cotter pin installed and one leg bent to hold it in position.

Washers (of thickness determined earlier) and bushing slid on.

1145257307_Uppersteeringshaftcotterpinwashersandbushinginstalled1.JPG.5cabc408fa6d7f728769407802666d94.JPG

336019689_Uppersteeringshaftcotterpinwashersandbushinginstalled2.JPG.ab413f60263fe4c4679a2e049c3c876f.JPG

 

Console placed back on ensuring bushing is properly seated and the Left side bolt screwed in finger tight.

Right side front bolt installed finger tight. This will be how this bolt will stay for now as it has ground wires and a clip to go under it as well at a later date.

 

PTO stop ready to be installed.

This gets bolted in to the Right side rear of console.

593572783_PTOstopreadytobeinstalled1.JPG.f4701d89d12fbaebd2b619691b005550.JPG

1237839947_PTOstopreadytobeinstalled2.JPG.7b7a5a61b5cf8b0992ce56bd7c77d1f8.JPG

 

PTO stop installed.

Rear console bolts both tightened.

1981356584_PTOstopinstalled1.JPG.ac9194e0e5ec4bb3196006e8f5ff5dd7.JPG

1690513738_PTOstopinstalled2.JPG.468489c9fb7cf6fdeb814c00dd3470c3.JPG

 

Console is now installed.

185558973_Consoleinstalled.JPG.afd51cf1ade8d1b872a0e769284c12a5.JPG

 

Overview as of today.

409418069_OverviewasofDec162025.JPG.3c40324acf4b3a112f6620e2b7d9e63a.JPG

 

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peter lena

@cleat  just have to say , lucky you  !  with your  interest / talent  and the abundance  of  hi end units , your  source / supply  will keep you  turning out  better than  original  horses , any  improvement  / change  only enhances your set ups .  way to go , pete

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cleat

Belt guard bracket and fuse holder bracket ready to bolt to front cover.

1015441022_Beltguardbracketandfuseholderbracketreadytobolttofrontcover.JPG.bfe8bdf3b38133fce456cc4aa9a47360.JPG

 

Belt guard bracket and fuse holder bracket bolted to front cover.

Bolts torqued to 96 in/lb.

1305774199_Beltguardbracketandfuseholderbracketboltedtofrontcover1.thumb.JPG.512790ee7319c8ba95039a1c85ece4f1.JPG

310269414_Beltguardbracketandfuseholderbracketboltedtofrontcover2.JPG.dd28931d4b7be631ab254bd9dcfbaa5c.JPG

1278906835_Beltguardbracketandfuseholderbracketboltedtofrontcover3.JPG.760b59a2ae33f8ca8d1ded48b53b03fe.JPG

 

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cleat

Front cover assembly ready to install.

1132811784_Frontcoverassemblyreadytoinstall.JPG.a8e481d534d7ce9d9fe49aa67b329c02.JPG

 

Tractor ready for front plate to be installed.

PTO rod supported by box to help prevent paint scratching if it were to hang down.

2008606602_Tractorreadyforfrontplatetobeinstalled.JPG.abefba02f52d3ad7856756b309ed5dc7.JPG

 

Front plate assembly installed and bolts tightened.

You will notice the Left side (as from seating position) fuse holder bracket bolt has been reversed as the nut on the backside was contacting the hydraulic valve fitting.

445857099_Frontplateassemblyinstalledandboltstightened1.JPG.f6d2c93adcfcd308577be686e7ba0621.JPG

1581153377_Frontplateassemblyinstalledandboltstightened2.JPG.7bf0157e994af44cc0f44402d4b1b553.JPG

 

PTO return spring ready to be installed.

1700801852_PTOreturnspringreadytobeinstalled.JPG.61e44d925d9e6d084eed11691a670439.JPG

 

PTO return spring hooked onto PTO control rod cotter pin.

821631125_PTOreturnspringhookedontoPTOcontrolrodcotterpin.JPG.665949380666f136c7e17a8d7a6a3a73.JPG

 

PTO return spring hooked onto belt guard bracket.

I used the same spring hook tool for this that I used for the foot control spring in an earlier post.

1346617270_PTOreturnspringhookedontobeltguardbracket1.JPG.2f7743210fde87fceb99b8d85fd98280.JPG

1745795477_PTOreturnspringhookedontobeltguardbracket2.JPG.0c5d58d72fd8b5447afbb1cf19242bb7.JPG

 

Overview as of today.

PTO return spring is now holding the rod up.

1674767078_Overviewasoftoday.JPG.184e5f2db3c51d7f6eec0862a231a687.JPG

 

Edited by cleat
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cleat

Well, my OCD kicked in and I switched the other bolt around so they would both be the same.

DSCN9816.JPG.88352e7fbbf3b988d9baa4b9d63554a5.JPG

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Bill D

Will those bolts contact the fuseblock if you leave them like that?

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cleat
25 minutes ago, Bill D said:

Will those bolts contact the fuseblock if you leave them like that?

 

Nope, not even close.

DSCN9817.JPG.531cf1e4b72377423b6f1566d53f8b4b.JPG

 

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